The Los Alamos Neutron Science Center (LANSCE) linac provides high power proton beams for neutron science, Tritium target development, nuclear physics, material science, isotope production, and weapons research. The number of simultaneous beam users places heavy demands on the RF powerplant, especially the 201.25 MHz power amplifiers (PA) driving four drift tube linac (DTL) tanks. Designed nearly 30 years ago, these amplifiers have operated at up to 3 Megawatts with duty factors of 12%. The large number of power tubes in the PA and Intermediate Power Amplifier (IPA) plate modulators, the age of the cooling and control subsystems, tube manufacturing problems, and operation near maximum PA tube ratings have all affected the system reliability.
By monitoring final power amplifier plate dissipation
and tube vacuum, improved operating procedures have raised RF
system reliability above 95% for operation periods in 1993-95.
Other recent modifications and upgrades to the 201.25 MHz RF
powerplant have significantly improved the operation. Higher
beam current for a proposed Long Pulse Spallation Source (LPSS)
cannot be delivered simultaneously with other beams at high duty
factor, however. Plans are underway to develop a new final power
amplifier which can use low-level RF modulation for amplitude
control. With only a few power tubes, the system will deliver
high peak power and duty factor, with improved DC to RF efficiency.
and a simplified cooling system.
A block diagram of the original 201.25 MHz RF system is shown in Figure 1. The maximum duty factor is 12% where the plate dissipation of the final amplifier tube (Burle Industries 7835 triode) is approximately 250 kW. A selection of the 7835 parameters is given in table 1. The peak power out of the final cavity amplifier is over 3.0 MW in some cases. The amplifier chain used a solid state preamplifier and a dual tube driver to provide 4 kW output. This output drives the IPA, a Burle 4616 tetrode, to achieve 130 kW. Finally the 7835 PA can deliver over 3 MW.
The 7835 cavity amplifier is unstable if operated with B+ but no RF drive, so the input high voltage is modulated by the amplitude control electronics in order to adjust the saturated output and thereby provide the amplitude control. This high voltage modulation technique requires four power tubes. The modulator has an internal voltage drop of 8 to 12 kV, so the high voltage capacitor bank must be maintained with that head room above the level needed by the 7835. At the present peak powers, the 7835's require 19 to 21 kV, and the capacitor bank operates at approximately 30 kV. Operation above this level not only stresses the capacitor bank and power supply, but stresses the modulator tubes.
Fig. 1. Original 201 MHz Amplifier System.
Type | Cathode-Driven Triode |
Gain | 13.6 dB |
Designed | 1960 |
Filament | Thoriated Tungsten |
Filament V | 4 V |
Filament I | 6800 A |
Plate Dissipation | 300 kW |
Plate Voltage Max | 40 kV |
Water Flow | 200 GPM |
The IPA high voltage is derived from the same high voltage as the PA. The IPA operates as a linear amplifier, so the high voltage is only switched on and off. Its level is not modulated as in the case of the final amplifier. A tube-based modulator is used to switch the high voltage on the 4616, requiring 3 power tubes (fig. 1).
In the original configuration, the entire 201.25
MHz amplifier system required thirteen power tubes per module
times four modules, or fifty-two power tubes. Recent modifications
have reduced that number to nine per module [1,2]. These included
the 1994 installation of a solid-state driver and a solid-state
screen grid (G2)
pulser for the IPA stage. These are included in fig. 2. An upgrade
is planned for the near future in which the IPA will have its
own high voltage power supply (HVPS). This will eliminate the
three-tube HV modulator and bring the total tube count per module
to six. When the IPA HVPS is installed the 201.25 MHz system
will be arranged as in Figure 2. This upgrade is just beginning
with the purchase of a prototype HVPS, due for arrival in late
1996.
Fig. 2. 'Upgraded' 201 MHz Amplifier System.
The original specification for the 7835 super power
triode lists the average plate dissipation limit of 300 kW (Table
1). LANSCE has operating experience which suggests that for safe
operation, dissipation should be below 250 kW. Real time monitoring
of the average plate power dissipation of the FPA was installed
in 1993 [3]. Using the temperature difference in the plate coolant
manifold and the flow from a sensor, the power wasted in the plate
coolant (plus a factor for filament and drive power) is computed
with an embedded controller and used for readout and interlock
of the HV. We implemented administrative controls to limit the
operation to plate dissipations of less than 250 kW. Catastrophic
failures have been significantly reduced. This is especially effective
during beam tuning and transient start-up conditions when the
RF power level is fluctuating and the resonance controller is
moving the DTL tuning slugs.
Another significant improvement was the addition
of peak power monitors (PPM) to indicate RF power levels in Watts
for the entire amplifier chain. The PPM replaced original uncalibrated
detector diodes and directional couplers which were only useful
for indicating that a signal was present. We purchased commercial
directional couplers in 5 kW, 150 kW, and 3 MW "sizes",
for the driver, IPA, and PA outputs, respectively. Lowpass filters
eliminate harmonics from the power signals. A PPM timing gate
allows sample/hold of the peak anywhere in the RF waveforms. These
signals are fed to large LED displays, and to the central control
room for logging. Both forward and reflected power are monitored,
using custom versions of the Narda 481 diode power monitors.
Linearity is ±0.25dB over a 10dB dynamic range.
The original 7835 PA filament supply was an unregulated,
variac-controlled supply. As noted in table 1 above, this supply
delivers over 30 kW of DC power. A modern SCR supply was purchased
for our test stand to see the benefits of filament current regulation.
The regulation has been shown to be effective in stabilizing the
7835 operation, since the cathode current in the grounded-grid
triode is proportional to emission from the filament. However,
because of the cost of the filament supply and the desire to replace
the 7835 amplifier stages in the near future (see below), we have
chosen to modify our existing supplies rather than make new purchases.
The modification consist of adding a control circuit to the power
supply which adjusts the variacs as the supply output current
varies. In order to avoid excessive brush wear in the variacs,
the control circuit is designed with an adjustable dead band.
We have found that 50A is a suitable band. The regulation is sufficient,
and the brush movement is not excessive. The regulator is isolated
and filtered to ignore the pulsed cathode bias voltage which is
common to both filament connections.
In 1992, analysis of the PA plate modulator output waveforms showed an undershoot of about 5 kV after pulse shutoff. The cutoff 7835 triode was acting as a rectifier for the returning RF power spike from the DTL tanks during decay. A high power clamp diode was connected from the floating deck to ground, eliminating the negative transient which was charging the deck. This modification dramatically reduced nuisance crowbars due to modulator tube faults. Current transformers were also added to monitor screen current and the plate current in each 4CW250,000B tetrode. These diagnostics have allowed us to predict when a driver or modulator tube is weakening and plan a changeout in advance [1, 2].
The modulator driver tetrode (4CX3000A) filament and screen power supplies were modified with the addition of ferroresonant (constant voltage) transformers. This stabilized the overall modulator loop gain for line voltage fluctuations, and has doubled driver tube lifetime by allowing us to hold closer tolerance to optimal filament temperature. Because of the screen voltage regulation, linac fill time is improved when the driver tetrode operates saturated.
We have installed new bias power supplies for the 4CW250,000B tetrode modulator tubes which allow a higher control grid bias: 500 versus 350 volts negative. This cuts off the tubes more completely during the beam-off time, to minimize cutting of the anode of the tube from the electron beam, which is focused in this condition. The new bias supplies are modular units which are very easy to replace compared to the original hard-wired supplies. Safety is enhanced with the new bias power supplies, and modulator tube life is extended.
The second stage of solid state amplification in
Figure 2 was a recent upgrade which replaced a dual-tube amplifier
[1]. The original Burle 7651 tetrode driver tubes had a short
lifetime due to a cooling design limitation. They were adequate
at low duty factor, but the present duty-factor raised the ceramic
seals in some units to near 250°C. New water-cooled solid
state amplifiers, using thirty-two Motorola MRF141G MOSFETs combined
to deliver up to 5500 W, were installed in 1993 and 1994. Reliability
is now excellent with these units. In addition, an entire rack
of power supplies, blowers, and amplifier cavities has been eliminated
for each 201.25 MHz amplifier system.
The first level of arc protection for the FPA and
IPA RF tubes is provided by a modulator blocking circuit. That
is, in the event of an RF tube arc, the modulator switch tubes
are shut off as rapidly as possible. In addition, the crowbar
trigger circuit waits on the order of 10 µs for the modulator
to extinguish the fault current before commanding the crowbar
to fire. This long delay time forces a requirement for a 10½
fault limiting resistor which must dissipate about 70 kW in normal
operation. The resistor is immersed in an oil tank, and the oil
is cooled by a heat exchanger external to the capacitor room.
Maintenance costs plus environment and safety concerns have pushed
us to consider an air-cooled resistor. Toward that end, we developed
a 3µs crowbar, with an amplitude threshold of about 3 kA
to work in conjunction with the existing crowbar in module two.
The fault limiting resistor is reduced to 3½ , dissipates
21 kW, and is air cooled. In addition to the crowbar and limiting
resistor improvements, we fitted each capacitor with a spring
loaded fuse to isolate the capacitor in the event of an internal
short. The new crowbar circuit will protect a 30 gauge wire; after
3 months of full operation, there has been no increase in the
number of crowbar faults in Module-two. The remaining three modules
are scheduled for similar upgrades in late 1997.
LANSCE is beginning to look into options for replacement of the 7835 PA stage. The primary goal would be to install a new cavity amplifier which will operate as a linear amplifier and eliminate the need for modulation of the high voltage. Modulation of the output power will be done with the RF drive to the preamplifier stage. This will eliminate four more tubes in the system, leaving only two RF amplifier tubes per module. In addition, the voltage overhead of the high voltage modulator will disappear (about 10 kV), so the capacitor bank and HVPS can operate at reduced voltage levels. We hope to be able to replace the 7835 with a single tube amplifier, but we are also considering the use of two tubes which are summed together in a hybrid combiner.
Cathode-driven tetrodes initially designed for fusion
heating are the likely choice. There are very few other super-power
VHF tubes capable of high duty factor like the 7835. With this
power source, we expect to be able to deliver up to 3.8 MW of
peak RF power at a duty factor of 15%. This would provide enough
RF for long pulse operation of the H+ beam at 21 mA, interleaved
with the H- beam for our proton storage ring. This work is in
the early stages of design.
Through continuous improvements, the LANSCE 201.25
MHz RF powerplant has reduced from using fifty-two power tubes
in 1992 to thirty-six in l996. Planned upgrades to the IPA and
PA stages to remove both plate modulators will reduce this number
to only the RF amplifiers themselves, with a total of eight tubes
being the optimal design for the high duty-factor requirements
of neutron science. Along with the reduction in power tubes,
improvements in operational procedures with new diagnostics, stabilization,
and protection circuitry have enabled the RF systems to function
with exceptional reliability in the past three years.
[1] W.M. Parsons J.T.M. Lyles, and H.W. Harris, "Modulation Improvements in the 201.25 MHz RF Generators at LAMPF," 20th International Power Modulator Symposium, Myrtle Beach, SC, June 23-25, 1992.
[2] W.M. Parsons, J.T.M. Lyles, and H.W. Harris, "Upgrading the LAMPF 201.25 MHz RF Generators", LA-UR-93-823.
[3] R. Cliff, E.D. Bush, R. A. DeHaven, H. W. Harris
and W.M. Parsons, "Developments and Directions in Two Hundred
Megahertz Very High Power RF at the Los Alamos Meson Physics Facility,"
RF Expo East, Orlando, FL, October 29, 1991.
* Work supported by the US Deparment of
Energy.